I have a 8v GU that's been running happily on a Weber 32/34 DMTL. I have just swapped out the 4-1 exhaust for a Corrado 4-2 manifold and a Frankenstein 2-1 downpipe.
As it's a Syncro the original down pipe was narrow and squared off due to lack of room. Now it's obviously breathing much better...so well, in fact, I can only get it to run if I fix the choke 80% closed.
It massively leans out with any throttle. I have checked:
Vacuum tubes - no leaks Carb/adapter/flange/manifold gaskets - no leaks Intake manifold - no leaks Exhaust manifold - no leaks Throttle plate on primary - centred and full closes Jets: increased the idle from 55 to 60 - no change in idle Cleaned out carb primary circuit - clean New fuel filter Timing checked - 8°BTDC Vacuum Guage 19.5 in HG Fuel pump - pumping Accelerator pump - pumping
I haven't had a chance to pull the plugs but I'd bet money on them looking lean.
I will check the float but it's only 6 months old and was set properly.
Maybe dirty needle valve?
I am at a loss as to what else it may be. Help me MK2 owners. You're my only hope...